KT100 rebuild

The main bearings are something I wasn’t expecting. The outer nylon shell around the outer race…what’s with that? The inner race can be move at a compound angle the center axis of the crank.
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A visual of the case before cleaning.
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My first guess with the nylon case on the bearing is to be able to press it in without heating the case?

IDK, I’ve never seen the sleeve but I’m no expert either… Could have been a case issue at some point that required machining out the pockets to a larger diameter. You’re allowed to machine the pockets to make sure they are true anyhow so as long as the bearing is snug in there you should be good.

Starting to see some wear on the crank from the main bearings, might be an opportunity to sleeve the crank and go to a 6205 bearing in it’s place.

Piston is def past it’s prime but the rest of the engine doesn’t really look bad at all.

Anybody have engine component dimensions?
Here’s what I’ve measured.
Endplay .014”

Base gasket .020”

Head gasket .015”

Piston 52.159mm 2.0535”

Cylinder 52.286mm 2.0585”

Clearance .127mm .005”

Crank journal PTO 19.974mm .7864”

Main bearing I.D. PTO 20.028mm .7885”

Crank journal IGN 19.979mm .7866”

Main bearing I.D. IGN 20.028mm.7885”

Seal journal PTO 19.903mm .7836”

Seal journal IGN 19.994mm .7872”

Piston pin 14.003mm .5513”

Piston pin boss 14.020 .552”

Rod small end 18.034mm .710”

Looks like the bore to rod alignment is off based on the loading to one side of the pin bosses. Not really concerned about it, not running in any competition with the engine. just going to use it for open practice for seat time to save wear on the Kohler race engine.
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Crank assy. is off to get split and new rod bearing installed, cylinder is going to be honed and piston fit at the same time. Main bearings are good to go. He said they are self-aligning and a more expensive type. Run’em. Crank journals are fine.
I’ll take delivery of that and additional parts at the swap meet next weekend, and start the assemble.
The piston wear at the pin boss is not uncommon. No big deal for my needs.

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Got the crank and cylinder back. Cylinder hone to fit new 52.20 piston ($25). New rod bearing installed on trued-up crank ($40). Started rebuild.
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New seals installed. Used Threebond 1184 for the case.
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New .020" base gasket and cylinder installed. Ready for cylinder head. Carb cleaned and rebuilt. Pop-off set to 10psi @ .040" fulcrum height without gasket. I used my dial caliper as a depth gauge across a straight edge when setting the fulcrum height. Once the caliper contacted arm and released pop pressure, measurement was recorded. This worked great!

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Thanks for documenting this and sharing it.
Was the rod checked for true and ovality?

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Combustion chamber cleaned up very nice, no pitting from detonation.
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After cleaning chamber I found that the S/P hole was helicoiled. Interesting that the heli depth is only .435" of the available .680" of overall thread depth. I think heat transfer would suffer from this lessened thread engagement. Also, looks like heli threads are getting old. Wonder if a second up-size heli is available? Something for doing a Heli a second time?
Notice thread condition…
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Yes, rod was check. And crank was trued on centers.

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Also, after I complete the assemble I’ll have the same engine builder run break-in and dyno pull.
I’ll share that too.

Thread repair inserts are out there.

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http://www.timesert.com/html/bigsert_sparkplug.html

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Great progress, I’m putting my backup KT100 together this week so going through much of this myself.

Timeserts are a MUCH better solution than helicoil, I wouldn’t hesitate to use them. I installed timeserts in the aluminum wheel uprights on my GT3 where the radial mount calipers mount because it’s a know weak point that can strip out easily. They have been in there for 4 years now and are holding up great.

Thanks and Andy. Check out this video link I posted.

I’m going to call the engine builder today and get he’s thoughts on this today. I can do the machine work myself in a mill at work. Pretty straight forward job, plunge mill out the old heli, drill and tap M18 x 1.5. Spotface & countersink for washer surface of insert. Use 266 loctite, good to go.
Only concern is if the installation tool is really needed for installing insert, if it’s tri-lobed to expand the bottom portion of the insert.

This is the old crank pin bearing and thrust washers.
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The old seals had grooves around the O.D. I like that idea with RTV. They also had the tension springs removed, probably to reduce drag.
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Everything looked good during disassembly. No red flags.
A name drop to Scott at Two Cycle Technology for the crank, cylinder work and parts.
I’ll report back with more, either dyno or head work (ordered Big-Sert inserts).

Wow, this is 5 years old. I have 2 KT100s sitting around and collecting dust. Going to do open them up and see if they need something new. Thanks, Dan for the info. I wonder if Two Cycle Tech is still working. Going to hit them up to truen my crank.

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